Ok, next up, the short stroke 750 was ready to go for Sept. ECTA meet. 850 cases & jugs, custom made Herb Becker short stroke billet crankshaft, Jim Schmidt Pistons, cam, rods and beehive springs, FullAuto head, custom porting and valves. Crank is 9lbs lighter than stock!
All Installed, dyno'd and ready to go.
Back to the Ohio MIle we go!
After a morning of rain, runs started at 2:30pm. First run had trouble getting into 2nd and 3rd gear. 127.1 MPH. Second run, again real trouble getting solidly into gear, missed 2nd gear again. wound up with a 127.8 mph. That was it for us on day 1. Clock wound out before we could get a 3rd run in. Back in the morning.
Next morning got on the line bright and early to a very chilly morning. Had the VM40s jetted to .300. Left the line and my helmet immediately fogged up, and was still not going into gear properly, so had to pedal the throttle a bit until I found a corner of my visor I could see through. Once I could see through a small spot, I got back on full throttle, but engine surged and would not climb past 6000rpm. Ran the trap at 106mph, so something was definitely up. Pulled back into the line up, and discussed. Herb thought it sounded like a possible scuffed piston, and wanted to hear the motor run. Upon hearing it, we pulled the plugs and without a compresssion tester with us (it was back in the pit), Herb did a "thumb test" while we turned the motor over, and sure enough, left cylinder had lost consderable compression. Out of line we went, back to the pit to pull the head and see what's up.
Sure enough, scuffed a piston. Upon pulling the head, it was apperant the left intake runner had come loose, so we figure that was enough to run that cylinder lean and cause the scuff. In all our haste to get to the start line after the rain on Friday, we didn't go through and "nut and bolt" the bike like usual, and then the morning was another rush to the start so we didn't loose our place, so again, no thorough "nut and bolt" check. Lesson learned. better late to the line than breaking stuff. Anyway, what to do?
Thankfully we brought the trusty 860 motor as a back up. an hour later, we where ready to rock (almost).
The crank taper on the billet 750 crank was just a bit longer than the taper on the stock crank in the 860, so the engine pulley hit the case before the taper made contact. Maybe we'de be done for the weekend...
But wait! We remembered a TSC store about a mile up the road. Herb and Bill jumped in the truck for a quick trip to get a sheet of .22g shim stock and a pair of tin snips. Some cutting, hammering, fitting and trimming later, the pulley was mounted and even lined up with the rear pulley! back in business! The new plan was now to try and bump our own record in the 1000cc class. We adusted the shift linkage and the position of the shift lever to try to get a more positive engagement, and once I felt I could really get it in gear properly, I took the bike for a spin around the pits to make sure everything was OK, and the bike seemd great. After a quick final inspection we got back in line.