- Joined
- Sep 18, 2014
- Messages
- 131
After some monkeying about with my wild running carb I found I had the slide on the Mukini upside down! Cue Fred Sanford, "You big dummy!". So this is sorted, then a new throttle cable had to be shortened an inch... So then off for a ride!
New brakes from Old Brits were installed a while ago with some minor issues, the result has been disappointing. The rotors still not scuffed off enough up front, the rear is useless. I used the old pads to remove the paint as per instruction from Fred. I'm sure it will take a little while to cut through the paint although the brake cleaner seemed to do a better job in places. I should have scuffed off the pads on my belt sander first and may do this tomorrow.
Brought her home from my pals place (gave me a hand with the carb) in Virginia back to Md, unloaded the old girl and went to start her up. No dice! No spark! Never an issue before... Old a Brits ignition was newly installed and worked perfectly.... So one step forward another back. I'm beginning to think this 75' MkIII is going to be my undoing.
I will the Avons did a nice job and the bike handles fairly well I think. I believe I need to investigate some clutch slippage and an oil leak beneath the primary case.
I'll pull the tank off and check all the grounds and connectors tomorrow, damnit, fall is here and I'm ready to ride!!!
New brakes from Old Brits were installed a while ago with some minor issues, the result has been disappointing. The rotors still not scuffed off enough up front, the rear is useless. I used the old pads to remove the paint as per instruction from Fred. I'm sure it will take a little while to cut through the paint although the brake cleaner seemed to do a better job in places. I should have scuffed off the pads on my belt sander first and may do this tomorrow.
Brought her home from my pals place (gave me a hand with the carb) in Virginia back to Md, unloaded the old girl and went to start her up. No dice! No spark! Never an issue before... Old a Brits ignition was newly installed and worked perfectly.... So one step forward another back. I'm beginning to think this 75' MkIII is going to be my undoing.
I will the Avons did a nice job and the bike handles fairly well I think. I believe I need to investigate some clutch slippage and an oil leak beneath the primary case.
I'll pull the tank off and check all the grounds and connectors tomorrow, damnit, fall is here and I'm ready to ride!!!