- Joined
- Dec 30, 2003
- Messages
- 3,689
I'm back again with a new string on Norris RX in my '72 750 combat engine. Took the opportunity to recheck cam timing while the head was off for oil leak fix. Used a really good set up this time and managed to get the intakes at 54degrees BTDC per spec. Go the whole thing back together and took a ride around the neighborhood. Loping idle was much less noticable, the mid range is back and nice power. Bad news was it ran so good I got carried away reving it too high and heard a bang. Blew a 3 inch piece of the new head gasket out the left side. Gotta go to Rabers and get a new gasket, but at least the cam timing seems to be working now.
After Raber's did a slight resurfacing of the head the front studs don't have enough threaded portion to tighten up the head. Need to put some thick washers in there to take up the space, then good to go.
After Raber's did a slight resurfacing of the head the front studs don't have enough threaded portion to tighten up the head. Need to put some thick washers in there to take up the space, then good to go.