Mk 2 Amal hanging up

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Dec 28, 2024
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Just finished refreshing my ‘72 750 Roadster which languished for too many years. Has less than 15K miles on a single Mk 2 Amal that I fitted in the 80s. Thoroughly cleaned the carb and installed all new jets, float, and needle. Everything works as advertised statically - cable moves smooth and freely and the slide snaps right back to the idle stop. 2 kick starter with a nice 900-1000 RPM idle. However…when revving it, it will NOT return to idle, almost wants to run away. It’s like the slide is hung up, but after shutting it off, the slide is sitting right on the idle stop. Side note: has a Tri Spark ignition.

Been through the remove/clean/install/test fire/fail scenario a couple of times - same result.

Any ideas/suggestions? Thanks -
 
Drop the idle stop by unscrewing, if the revs stay high you have an air leak. To find the airleak spray wd40 or similar over the manifold joints, when the spray finds the leak the revs will change.
 
Just finished refreshing my ‘72 750 Roadster which languished for too many years. Has less than 15K miles on a single Mk 2 Amal that I fitted in the 80s. Thoroughly cleaned the carb and installed all new jets, float, and needle. Everything works as advertised statically - cable moves smooth and freely and the slide snaps right back to the idle stop. 2 kick starter with a nice 900-1000 RPM idle. However…when revving it, it will NOT return to idle, almost wants to run away. It’s like the slide is hung up, but after shutting it off, the slide is sitting right on the idle stop. Side note: has a Tri Spark ignition.

Been through the remove/clean/install/test fire/fail scenario a couple of times - same result.

Any ideas/suggestions? Thanks -
Are you absolutely certain the slide is on the idle stop when the revs are climbing?
My single carb mikuni used to do exactly that until I fitted an extra return spring
If not that then you are pulling air somewhere
 
With a single carb the cable is very close to the frame spine (unless the carb is angled slightly) so it could also be the cable causing it to hang up slightly.
 
Drop the idle stop by unscrewing, if the revs stay high you have an air leak. To find the airleak spray wd40 or similar over the manifold joints, when the spray finds the leak the revs will change.
Thought about the air leak - replaced the mankey spigot mount. Will idle smoothly about 900 or so until ref’s over 1600/2000, then not come down. Still a mystery
 
With a single carb the cable is very close to the frame spine (unless the carb is angled slightly) so it could also be the cable causing it to hang up slightly.
Yeah, the routing is ideal but the slide is snapping right back to the idle screw….at least statically.
 
I have just had a similar experience with my T150, did all the obvious things and eventually replaced the throttle cable which sorted it out. On close examination I found that the inner had a single strand starting to separate, but it was not visible.
 
If after checking all of the above and making sure the slide is clean...
It could be a vacuum issue with the round slide.
Mikuni overcame this issue with the 'Heavy' brass, chrome plated slide.
They and Keihin also went to flat slides.
A heavier or newer spring may be in order.
 
Had not thought of that…and…not sure how to identify and cure that?
If the carb has age to it - change it. I've fought both MK2 and Mikuni due to them. Of course, you can remove it and look at it - pretty easy. The seal can be bad or it can be hanging up. It makes the carb too rich but then people compensate so it becomes very confusing.

One check is to get it started and warmed up, then open and close it - should make a BIG difference if it is working correctly. If it's leaking, then little to no change.
 
If your slide is sitting on the idle stop and you are not touching the throttle and the revs climb then you have an air leak
Any other scenario points to the throttle slide or cable hanging up
If you had a mechanical advance I'd say check that too
But you have an electronic advance
 
If your slide is sitting on the idle stop and you are not touching the throttle and the revs climb then you have an air leak
Any other scenario points to the throttle slide or cable hanging up
If you had a mechanical advance I'd say check that too
But you have an electronic advance
Have a fresh spigot, which I believe is well-sealed to the head. The cable moves smoothly throughout the range, but I might try a new one.

Thanks to all who’ve responded - it’s good having an experienced community available to bounce off.
 
Drop the idle stop by unscrewing, if the revs stay high you have an air leak. To find the airleak spray wd40 or similar over the manifold joints, when the spray finds the leak the revs will change.
Make sure you don't have too much outer cable clearance, because sometimes the Ferrell can sit a little cocked if it comes out of it hole too much. Cheers
 
I have no love for the MK2 carb. I have heard / read of very good running MK 2 carbs but never experienced it. Best thing you can do...buy a single Mikuni replacement and your problems are gone. Give the MK 2 a whack with a hammer for me.
Well I’ve had great results with many MK2s over the years.

There is nothing special / mystical about them. Excluding the cold start system, they operate very much like MK1s. Remember, they were the carb of choice for racers and tuners for many years, from Italian scooters to big Japanese superbikes.

I believe the issues arise as a result of what Meriden and Amal did with the T140E in order to squeeze a dinosaur bike through stringent EPA rules. They did rather unusual things to the carb settings, but the carbs do work well in EPA spec, albeit they work better in none EPA spec.

The issues arise when you’re in between. If any one of those things is missed or miss understood and you end up with a kind of hybrid EPA / non EPA set up you can be chasing your tail to the extent you think you’re going crazy!

I was there with my current T140 when I first bought it. In desperation I even bought a new set of MK1.5 carbs. IIRC Burlen also confuse things with some setting errors / differences. But once I’d got the MK2s sorted as per the recommendations of John Healey, they performed just fine.
 
The first set of MK2 carbs I fought was on a t140. I assumed that some one, somewhere had all the answers...I just needed to find him. I talked to truly knowledgeable people..I went the full jetting change euro to usa. ZIP. To make a long story short, I discovered the choke system is the big culprit. It is a massive fuel and air leak. The bike would not idle below 2500. It was completely unresponsive to the air mixture screw. I used new choke plungers...nothing. Finally I stuffed toilet paper into any orifice that fed fuel or air to the choke circuit and what a surprise..... it now behaved like a normal carburetor. However I ran into a pair of good used normal concentrics so I used those. Now they have potential. If you could block off the choke circuit and somehow provide a tickler I think they could be used.
BUT.....when a bike arrives with dual MK2 carbs I tell the owner there's only a slim chance they will ever work. I make a half-hearted attempt to use them but that's it. After spending several wasted months with the T140 I learned my lesson.
My theory is that there were good batches and bad batches made. Jaye says the ones built in Spain were the bad ones.
 
Just finished refreshing my ‘72 750 Roadster which languished for too many years. Has less than 15K miles on a single Mk 2 Amal that I fitted in the 80s. Thoroughly cleaned the carb and installed all new jets, float, and needle. Everything works as advertised statically - cable moves smooth and freely and the slide snaps right back to the idle stop. 2 kick starter with a nice 900-1000 RPM idle. However…when revving it, it will NOT return to idle, almost wants to run away. It’s like the slide is hung up, but after shutting it off, the slide is sitting right on the idle stop. Side note: has a Tri Spark ignition.

Been through the remove/clean/install/test fire/fail scenario a couple of times - same result.

Any ideas/suggestions? Thanks -
Appears it was a loose nut (yeahs the one behind the handle bars!). The ferrel at the twist grip was catching just enough when running to to hang the slide off the stop. Cheap and easy fix. Thanks to all who weighed in.
 
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