- Joined
- Mar 8, 2015
- Messages
- 38
Need some help after I have now ruined a fresh rebuild on a 68 Lightning. Bought as a basket case and no history on the motor.
I rebuilt the motor- new standard bearings, 20 over pistons etc. Timing side bushing looks good and measures right at the max tolerance. It did not have much play with the crank installed, so decided to run with it for now.
Got the engine running great and put about 20-30 miles on it and noticed a knocking. Decided to tear it down and both connecting rod bearings are now ruined along with scoring on the crank. Seems like low oil pressure but can't find a reason why. I had oil returning to the oil tank. The OPRV is the piston style that has the external pin that moves showing pressure. While cold the pin was out like expected and went in almost all the way when warmed.
Sludge trap was cleaned during the rebuild. I can blow air through the crank from the bushing side through to the journals. No restrictions. I used the original oil pump that I fed with oil while spinning to test. It spins and gurgles and seems fine. I took apart the OPRV and it seems fine. Spring has lots of resistance and the piston moves freely in the bore.
With the oil pump off, I blew air through each of the holes to confirm the passages were clear.
I'm totally lost as to why this happened. Without having a cause, I'm thinking about buying a new oil pump and OPRV and hoping this does not happen again. Any other ideas that I'm not thinking of?
I rebuilt the motor- new standard bearings, 20 over pistons etc. Timing side bushing looks good and measures right at the max tolerance. It did not have much play with the crank installed, so decided to run with it for now.
Got the engine running great and put about 20-30 miles on it and noticed a knocking. Decided to tear it down and both connecting rod bearings are now ruined along with scoring on the crank. Seems like low oil pressure but can't find a reason why. I had oil returning to the oil tank. The OPRV is the piston style that has the external pin that moves showing pressure. While cold the pin was out like expected and went in almost all the way when warmed.
Sludge trap was cleaned during the rebuild. I can blow air through the crank from the bushing side through to the journals. No restrictions. I used the original oil pump that I fed with oil while spinning to test. It spins and gurgles and seems fine. I took apart the OPRV and it seems fine. Spring has lots of resistance and the piston moves freely in the bore.
With the oil pump off, I blew air through each of the holes to confirm the passages were clear.
I'm totally lost as to why this happened. Without having a cause, I'm thinking about buying a new oil pump and OPRV and hoping this does not happen again. Any other ideas that I'm not thinking of?