My final, rambling stream of consciousness as I finish this project at the last minute:
In my head this is a really long story so I’ll trim it to the basics. After remembering that I installed used pilot jets, then swapping to new ones, the pilot circuit tuned in nicely. The only other change I made was to raise the needles one notch (richer slide & main jets were both bad moves).
The more I think about it, I believe the detonation is caused by other things and I might try to wean it off the good gas after this weekend. I did make the leap to running VP110 diluted down to 95+.
During tuning this weekend, I found both carbs loose, probably happened while riding the weekend prior. This isn’t new to me as I tend to be cautious about warping the carbs so I end up under tightening them; now properly torqued and loctited.
Toward the end of tuning I found a new oil leak under the magneto - lower mag screw came loose. On repairing this I found the mag chain tension sloppy & all fasteners loose, which I think could advance the timing a few degrees. In this case I used a very soft gasket under the mag that tends to extrude & relax over time, relieving tension on the fasteners. Again, torqued & loctited & timing reset to 28 degrees.
Then as a last FU, the threads at the rocker oil feed connection gave up and I had to repair that with a helicoil.
Do or die, I’m out of time
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Chris