- Joined
- May 30, 2019
- Messages
- 76
Need some insight as to cause of issue with fitting the outer primary cover on my 1974 Commando 850.
I installed a new AN inner cover. No issues with installation.
After completion of clutch and alternator install I installed my old outer cover without the rubber o’ring and checked for clearances. No issues, dowels and center bolt lined-up perfectly, cover seated with no gap to inner cover. Rotation of engine and clutch showed no touch conditions.
Installed outer cover with AN o’ring installed on inner cover. O’ring fit into groove was good – held in place without any additional sealant. Installed outer cover, torqued center bolt to 25 lb-ft. There is a consistent .030 to.050 gap all around cover interface. Increased torque to 30 lb-ft. No change in gap. I let sit overnight in that state to see if any relaxation in joint (didn’t think there would be). Checked next morning – same gap, application of torque didn’t change gap.
O’ring is compliant (don’t know durometer) but in good shape (new). Ends where glued together match perfectly. Diameter is approximately .220”.
Inner cover cast-in o’ring groove is clean with nominal depth of .115”. Seems shallow for diameter of o’ring but not sure what design intent is.
Assuming parts are all correct – any suggestions?
I installed a new AN inner cover. No issues with installation.
After completion of clutch and alternator install I installed my old outer cover without the rubber o’ring and checked for clearances. No issues, dowels and center bolt lined-up perfectly, cover seated with no gap to inner cover. Rotation of engine and clutch showed no touch conditions.
Installed outer cover with AN o’ring installed on inner cover. O’ring fit into groove was good – held in place without any additional sealant. Installed outer cover, torqued center bolt to 25 lb-ft. There is a consistent .030 to.050 gap all around cover interface. Increased torque to 30 lb-ft. No change in gap. I let sit overnight in that state to see if any relaxation in joint (didn’t think there would be). Checked next morning – same gap, application of torque didn’t change gap.
O’ring is compliant (don’t know durometer) but in good shape (new). Ends where glued together match perfectly. Diameter is approximately .220”.
Inner cover cast-in o’ring groove is clean with nominal depth of .115”. Seems shallow for diameter of o’ring but not sure what design intent is.
Assuming parts are all correct – any suggestions?