I just installed a Tri-Spark this week after not being happy with the performance of my Mk4 Boyer (the Mk3 seemed to work better IMHO, but that is another story). BTW - impressed with the Tri-spark.
I had the dreaded Podtronic installed, and yes the 3-4000 RPM light throttle miss did appear. I tried the filter fix (my local parts supplier carries them). Not really that impressed with the 18 AWG wire, but on with the show.
Being a skeptic, I popped some spade terminals on the ends so that I could hook it in temporarily to the red wire off the Podronic to test it's function without drastic alterations to the bike.
First thing I noticed - the miss is gone. Second thing I noticed - alternator charging is gone too!! Checked continuity and resistance through the filter - about 0.5 Ohm resistance. Reconnected Podronic without the filter - Charging system works, miss is back.
I tried connecting the filter into the black wire - same results.
I then connected the filter inline with the power lead to the Tri-spark. Miss is 75% gone - charging system works.
Finally, I dug out a square rectifier and a zener diode, pulled the Podronic, installed the rectifier and zener - problem solved. Plus side is, the alternator voltage seems better with the diode and zener.
Should have just done that in the first place.... Story of my life....
FWIW