I have a 750 Norton Commando that is completely restored. It sat on the work table for a couple of years while I constructed my Triton and recently came back to it.
I left the project as the damn thing would not start on the single Mikuni. The other day, I cleaned the carb, put fresh fuel in it, adjusted the air and fuel to a starting point and low and behold it started and sounded great. The problem started when I turned off the key. It did not stop. The running engine became erratic and when I turned the key back on, it ran fine again. I think somehow the stator was firing the engine. I installed a Boyer Micro-Power ignition and a Podtronics rectifier in the system.
I opened up the wiring and can see nothing that I did wrong - so far. Anyone out there ever experience anything like this? The only thing that had me curious was the stator wiring was interfering with the drive chain which if it cut through could charge the frame but I see no evidence where the insulation had cut through.
Once I get through the electrical mystery, there came another issue that I thought was behind me.
The two forward head bolts between the pushrods are weeping oil at the nuts. I have pulled the head put a new annealed copper gasket coated with NAPA copper flake gasket sealant before reassembly but it still leaks oil from these two nuts. Has anyone tried a thread sealant and copper crush rings under the nuts to seal this area?
The engine is very strong with no smoke and I know that once I get these two things behind me, I will have a machine that will do its best to put me in an early grave.
I left the project as the damn thing would not start on the single Mikuni. The other day, I cleaned the carb, put fresh fuel in it, adjusted the air and fuel to a starting point and low and behold it started and sounded great. The problem started when I turned off the key. It did not stop. The running engine became erratic and when I turned the key back on, it ran fine again. I think somehow the stator was firing the engine. I installed a Boyer Micro-Power ignition and a Podtronics rectifier in the system.
I opened up the wiring and can see nothing that I did wrong - so far. Anyone out there ever experience anything like this? The only thing that had me curious was the stator wiring was interfering with the drive chain which if it cut through could charge the frame but I see no evidence where the insulation had cut through.
Once I get through the electrical mystery, there came another issue that I thought was behind me.
The two forward head bolts between the pushrods are weeping oil at the nuts. I have pulled the head put a new annealed copper gasket coated with NAPA copper flake gasket sealant before reassembly but it still leaks oil from these two nuts. Has anyone tried a thread sealant and copper crush rings under the nuts to seal this area?
The engine is very strong with no smoke and I know that once I get these two things behind me, I will have a machine that will do its best to put me in an early grave.